Short flight near my home before sunset. I flew four batteries, at the last one the motor jumped out of its holder which ended in a crash. The rest of the copter didn't took any damage, so it should be easy to fix! :-)
I used amir's controller with default settings on HW 0.22, SW 0.59. The copter was pretty heavy with my big battery and the GoPro HD camera... I should trim my settings for such a high load.