After 7 hours of testflights the last days I have had a bad accident yesterday. The first 7 hours of testflights were perfect stable also attitude is brilliant.
Yesterday I lost the control of the copter after 20 seconds of flight. The flight was complete in Atti mode (no GPS). The octo doesn’t react on my commands or respectively very very delayed. Also as I lowered the throttle there was no reaction.
- Oktokopter with 6kg
- Wookong M
- Herkules III
- iOSD II
- Flight only in Atti Mode
- 2 x 4S 5.300 Lipos (fully charged)
- Receiver Jeti R10